Opua, New Zealand
03/15/2008 - 04/20/2008
We arrived in Opua a few days earlier than planned anxious to get started on the new generator install project. The project task list included remove the old genset from Whisper, clean up the engine room, prep the space to receive the new genset, upgrade the fuel delivery system, clean the old sooty exhaust system out, get the new generator in the boat, installed, tested, and working to our satisfaction — in just a few weeks. We had two weeks scheduled at the Ashby's boat yard work dock (which extended to almost three weeks) and lots of other work to do before leaving for Fiji.
Home sweet home — Ashby's boatyard will be Whisper's home for almost three weeks while we install the new genset, a DCGen 482M-12/200 from Onsite Power Systems in Coomera, Australia.
Although Whisper is at the far end of the work dock, she is farther away from the dust, dirt, and noise from the main boatyard. While Duncan works on installing the new genset, Robin will clean the dinghy, do the varnishing, and perform myriad pre-passage-preparation chores.
In preparation, Duncan disconnected the Fischer Panda and wrapped it all up ready to remove. Lowes Marine Services in Opua will help Duncan pull the dead Fischer Panda out of the boat. Duncan also placed a very honest classified out on TradeMe (New Zealand's version of an eBay-like auction site). This non-working $10,000 US genset eventually sells to a nice DIY Kiwi bloke in Whangarei for $660 US dollars.
Step two — Over the top of the Volvo (thanks to Luis!), out of the engine room, in front of the companionway stairs, then up and out of the companionway and into the cockpit. Dean and Luis from Lowes did most of the heavy lifting, while Duncan ran around making sure nothing got dented. Duncan rigged this block-and-tackle from old running backstays to get the 200 pound genset into the cockpit.
The Fischer Panda is on its way out of Whisper and in the cockpit. Duncan's smile of relief and joy is telling!
Dean and Luis from Lowes said "they had never seen anyone so happy to see the back-end of a marine system". Lowes stored the unit until it sold on TradeMe. It's a good thing we got it off Whisper when we did, the new genset arrived air-freight from Australia that afternoon!
But first, some clean-up to do! The platform in the engine room needs a good cleaning and tidy-up before moving in the new generator.
After cleaning, bring on the new generator. Patching cleans-up all the various screw and bolt holes. The platform is not removable — it's painted and epoxied-in 1-inch marine plywood.
A major day-long project (done a couple days before the Fischer Panda came out) involved up-sizing the fuel input line from 1/4" to 5/16". The 1/4" fuel return line size did not require change.
Fuel System Upgrade
The only system that required upgrading from the original Fischer Panda installation was the intake fuel line. All other systems — exhaust (1.5"), electrical (4/0 AWG), raw-water cooling (3/4"), anti-siphon (1/2"), and fuel return line (1/4") were sufficient for the new generator.
The fuel line replacement project required that the main salon floor be removed. The floor cannot come out without first removing the dining table. The dining table contains over a case of wine/spirits and is quite bulky and heavy (on the settee in the photo, right), but once removed, the fuel lines are easy to trace, disconnect, thread new, and re-connect. However, running this one new fuel line took almost an entire day from start to finish.
A later addition to the fuel system was a manually-switched 4-6 psi fuel pump. Adding a 30A relay and a basic wiring diagram for an automated on/off switch is on the future project list, but the manual switch works fine for now. Upgrading the inexpensive automotive fuel pump to a nice Facet pump is also on the list of "future" projects.
The new genset arrived at Lowes Marine Services in Opua that afternoon. The DCGen weighed just a bit more than the old generator and was larger (bulkier). In order to fit it into the engine room without harming either Whisper's main Volvo engine or the new DCGen, Duncan removed as many components as possible to reduce the size and weight.
DCGen 482M-12/200 Genset Arrives!
On the same afternoon the Panda came off the boat, the new DCGen arrived in Opua. Good timing, huh? The platform was clean, the fuel system upgrade was complete, and the boat was ready to receive the new DCGen482 solution.
As a quick recap, the DCGen 482 from Onsite Power Systems in Australia (sold through PowerStream) is a 12V DC genset. It's a Kubota 482 2-cylinder diesel engine direct driving (via a spider coupling) a large hot-rated (to 205F) 200 amp Prestolite alternator. The alternator is the same one used worldwide on emergency vehicles and RV's and can be configured as an N-type with a built-in regulator and/or external regulator (default, and most common in Europe/UK), or easily converted to a P-type alternator with an external regulator only (common in America and New Zealand). As we roughly understand it a P-type is wired with the voltage regulation upstream on Positive brush or an N-type downstream on negative brush. Or something like that.
Here is the alternator all wired up by Onsite Power to the Sterling Pro Digital Alternator Regulator. A new white "field wire" added to enable the Sterling regulator to externally regulate the voltage and amps delivered to the batteries.
The genset starts and runs at a preset throttle level providing 8-12 horsepower at around 2800-2900 rpms and consumes fuel (with slightly fluctuating rpm) based on the alternator loading. A 200 amp alternator requires a minimum 8HP motor, so the Kubota 482 is a good match. Because it is direct drive and there is no 3:1 pully driving the alternator up to 4500-6000 RPM (at 1500-2000 engine rpm) as with most engine alternators, the sustained amp output sits comfortably around 180 amps (200 when cold, 180 when hot). Fuel consumption is approximately 1 liter per hour at the 2800 rpm setting. That's enough on this for now, back to the installation...
This is the top-down view of the new genset on the shipping crate platform. The platform on the right is where accessory watermaker, refrigeration, or hydraulic pumps can be mounted and dual-belt driven. At some point, we might add a hydraulic pump and remote motor to drive a dive compressor.
Onsite Power had some issues with their custom exhaust-cooler/coolant-reservoir/heat exchanger during testing (it had a leak somewhere internally). We initially feared there was going to be a delay in the delivery while they manufactured and tested a new one. Instead, they got creative, went simple, removed the custom heat exchanger form the alloy casing, welded on some end caps, and gave us an off-the-shelf Bowman heat exchanger mounted externally instead. Duncan prefers this solution over the complex custom bits.
Lowes allowed Duncan to do the genset strip-down in their shop. Off came the air intake hose and silencer, raw water pump, and oil changer pump.
Then the coolant-reservoir, exhaust elbow, and heat exchanger are all removed.
The mini-alternator and mount (used to charge the start battery) are also removed. At this point, there was only an engine core, frame, and alternator. The unit weighed significantly less and would now be easier to maneuver into Whisper's engine room.
The DCGen arrived at Whisper with Dean and Luis from Lowes the next morning. Here, Duncan proposes a strategy for tipping the genset on it's side to get it over the top of the Volvo without damaging anything.
Once the DCGen was in the cockpit, we lowered it down the companionway and into the boat with the same block-and tackle used to lift out the Fischer Panda.
Ready to go. It is about ten more feet to go before the hard part — getting it over the engine and into the back of the engine room.
Luis had the hard job of the contortionist and receiver of the genset. Crouched in the engine room behind the Volvo, he received and guided-in the genset as Dean and Duncan slid it across the top of the Volvo on a thick layer of cardboard. Here is the unit positioned near its final position on the platform behind the main Volvo engine. Now the reassembly can begin.
After only a few hours, Duncan had the genset re-assembled and ready to move into its final mounting position. He wanted to get all the pieces in place to ensure clearances were sufficient around the unit. A critical requirement is ease of maintenance. Duncan decided on transverse mounting of the genset, keeping all the frequently accessed parts of the engine where they would be easy to inspect and reach for preventive maintenance.
It's Alive!
First, Duncan mounted the new DCGen in place. The base-frame/engine mounts were carefully positioned, marked, shifted, drilled, shifted back, bolted, and/or lag-screwed down to the platform. Amazingly, all the holes lined up and the unit ended up correctly positioned in the available space.
Duncan then connected the fuel, exhaust, cooling, and electrical systems, and began the process of start-up testing. After filling the unit with coolant and oil, bleeding the fuel system (a simple process on the 482), and checking everything twice, it was time to get the engine running. It started and ran fine, but the raw water was not flowing. Simple explanation, the raw-water pump was mounted incorrectly. Flipped it around the other way swapping the in/out ports and it worked fine! Imagine that. After just a couple days the engine was running and the alternator was actually putting out some amps. GREAT! However, it would be almost a month later before Duncan finished tweaking, debugging and could call the installation "complete".
This Sterling Pro Digital Alternator regulator looked like it was working (according to it's LED status lighting), but it really wasn't. There was very little troubleshooting or documentation to help us get to the root cause of the problem. The alternator seemed to be working and putting out 14.1V, but we suspected it was only running on its internal regulator. Disconnecting the Sterling PDAR had no effect, confirming it was only running on the internal regulator. This initially pointed to a problem with the Sterling regulator and not the alternator. Unfortunately, this was a red herring.
Sterling Pro Digital Alternator Regulator (PDAR)
Although the engine was running and the alternator was putting out some decent amps (just over 200 when cold), we realized after a couple of test runs that the voltage never climbed above 14.1 volts. The PDAR regulator was wired and configured correctly for our batteries. It should have been cranking out 14.7 volts. It wasn't. Why not?
This problem was the biggest hassle of the installation and delayed things by at least a week. Without going into all the detail about the symptoms, lack of information, misinformation, local NZ electrician opinions, the manufacturer's response to their opinions, Sterling Pro's response to any of the issues, and our reactions to all their various responses — suffice to say we eventually go down a different path.
Onsite Power was very supportive and quickly sent another PDAR to try, but they were not confident it would solve our problem — and in the end, it did not. Onsite did not, however, have great documentation, troubleshooting, wiring diagrams, or support for this particular electrical problem — and therefore we had a hard time narrowing down the root cause of the issue. The New Zealand local marine electricians would not even look at an N-type alternator, because 99% of what they deal with is P-type (usually Balmar).
Duncan needed to ensure this fuse-jumper for either an N-type (regulation controlled downstream on the negative brush) or P-type (regulation controlled upstream on Positive brush) alternator. We knew the alternator was an N-type, but look closely at the conflicting label and circuit board Positive and Negative labels. Duncan thought this might be the issue — a manufacturing defect. The manufacturer sent a new PDAR unit. In the end, it was not the problem. The second unit (labeled correctly) did not control the alternator either.
For a moment, Duncan thought the internal regulator on the alternator was an adjustable kind and needed to be tweaked a bit higher (like 14.25 volts) in order to trip-on the Sterling Pro. This was according to a guy on a Canal Boat Forum that had just installed one on his boat. Maybe this was the problem? If the internal regulator never made it to 14.25V, it would never kick-on.
When we attempted to confirm behavior this with Sterling, the note back from Charles Sterling indicated we could "tell the person [on the forum] they are an idiot" and we should use his name when posting. There was no explanation provided of how the Sterling PDAR actually did work, and no additional information or documentation provided that might help debug our problem. Very helpful.
In the end, the insufficient voltage probably had nothing to do with the Sterling regulator (the problem was a wiring issue with the field wire on the internal regulator), but the level of support and information forthcoming from Sterling made us uncomfortable, so we looked for alternatives.
In contrast, Prestolite support was a DREAM and we were extremely impressed with the level of knowledge, information, and support provided. Plus, their product seems to be excellent as well. We learned their alternators can be either a P-Type or N-type! This opens up some good alternatives.
Next step, we needed to ensure the field wire was still connected correctly inside the internal voltage regulator. Onsite Power does this as a part of the assembly. This required removing the alternator from the genset frame. It is easier to work on when removed and fairly easy to remove and replace — held in-place by three large bolts. Since there is no adjustment when using direct drive, the bolts and frame hold everything in perfect alignment.
When the internal alternator regulator comes off, out pop the brushes and brush springs. The white field wire was disconnected. The small solder-point had broken off one of the wire tabs.
The internal regulator, it turns out, was NOT adjustable and would only put out a maximum of 14.1V. We need a bulk charging voltage of 14.7V at 70F. Somehow, we either needed to get the Sterling PDAR working, or go another route. It was starting to worry us that our cruising season might be in jeopardy!
Duncan found the field wire just hanging there inside the internal regulator. He found a broken solder point, and thought "I'll just reconnect it where it was connected". Either it was always wired incorrectly by Onsite Power, or Duncan re-wired it incorrectly. Either way, it was frustrating not to have a wiring diagram to help troubleshoot.
If the broken solder-point on the negative regulator power wire (instead of a brush post) was a valid the indicator of where it was connected — the field wire was wired up incorrectly at the factory. We never did receive a wiring diagram that indicated exactly where the field wire should be connected, but it should probably have been somehow connected to the negative-side brush contact. The electrician that eventually helped solve this problem confirmed it was in fact wired incorrectly — it was soldered to a tab on the regulator power ground instead of the negative brush post. This would short the field to ground and an external regulator would never work correctly. Well, that explains some things.
We put the alternator on the local electrician's test bench. He looked at the internal regulator, and confirmed the field wire was wired incorrectly. After a quick discussion of options, we decided to change the N-type Prestolite to a P-type. We had a spare Balmar MC-412 voltage regulator that we know can deliver 14.7 volts. The electrician quickly converted the alternator to a P-type by replacing the internal N-type regulator with a simple mounting plate and brush-contact assembly ($65 US). We kept the internal regulator if we ever need a an emergency 14.1 volt output. We connected everything up and cranked it on with the Balmar MC-412 voltage regulator and got 14.7 volts! Progress!
Ready for the first at-anchor testing, things seemed to be working fairly well. Only one issue. The Balmar seemed to have a "pulsing problem" (+/- 20 amp swings) when it reached bulk charging voltage, so the first thought was it might be overheating. We moved it outside the engine room. Nope, still had the pulsing problem.
Finally after reaching the end of our troubleshooting rope, a local electrician put the alternator on his test bench. He quickly converted the alternator to a P-type with this simple mounting plate and brush-contact assembly he made. We connected-up our spare Balmar MC-412 voltage regulator and we got 14.7 volts and 175-200 amps, no problem. We were back in business.
As an aside, we learned from Prestolite support they offer an off-the-shelf part to easily convert their alternators to P-type. They also offer a Prestolite branded OEM external P-Type regulator made by Balmar. They have had good luck with this configuration on marine and RV installations, and based on our final solution, we believe them. If we had easy, quick access to these Prestolite parts, we might have purchased and used them instead of building our own solution.
Now that we finally had a working solution (that used the exact same model voltage regulator as our main engine alternator), we started to feel like we were making progress in the right direction again. We bought another spare Balmar ARS-5 regulator, and believe we now have a decent solution that will work long term.
We shipped all the Sterling stuff back to Onsite Power and got a prompt refund.
Now mounted in this cabinet and outside the engine room we still had the pulsing problem. Of course, it took another few days to debug this one. Balmar support helped and indicated the voltage-sense/power (red) wire was too small for the 20 foot wire run. Duncan up-sized the wire to 6 AWG and it works fine. Duncan also extended the temperature compensation wire by a few feet and connected it to a battery in the center of the house bank.
The standard face plate for the DCGen would not cover the old hole cut for the Fischer Panda control panel. We had a larger backing plate made and epoxied the DCGen plate within it. The manual switch (lower right) is the fuel-pump switch for the fuel pump.
Almost done — but not quite. We still needed to add a fuel pump, re-plumb the freshwater cooling side through the hot water heater, replace some crushed heating ducts (crushed during Fischer Panda maintenance days), and fasten all wires, ducts, hoses, fuel lines, etc. more securely in preparation for being at sea.
Although Duncan designed a Kubota/Volvo cooling system switching/bypass manifold, we decided to keep it simple and just splice into the genset cooling between the output and the external heat exchanger. Only the genset will heat water. Easy peasy. Duncan ensured all air bubbles are purged using the purge valves already plumbed on the water heater.
Replacing the old heater duct was supposed to be a low priority project, but after a few evenings in Opua with the temperatures dipping into the low 50's F, it was time to get the Webasto forced-air heater working again.
Installation Complete, sort of...
Duncan wanted to do this generator installation himself for two reasons. First, he would be intimately familiar with the unit by the time it was all done, and second, we did not want to pay someone several thousand dollars for the installation.
Additionally, we spent only about $850 on parts. It took Duncan much longer to install and debug than expected (overall about 4 weeks, including 2 weeks of testing time at anchor), but we saved some money and Duncan now knows the unit very well.
Some of the other mini-projects we worked or started during this install are outlined here:
We added an external 4-6 psi fuel pump as a fuel booster pump. We had a spare fuel pump from our last round of Fischer Panda fuel pressure testing, so used it for this purpose. In retrospect, we probably would spend the money on a Facet pump. The current pump has an integrated 50 micron filter which is not necessary (it's between the tank and the 2-micron Racor filter). Currently, this pump is manually switched. We have the parts (wiring/relay) needed to automate the on/off switching of this pump, but have not yet installed them.
Duncan modified the stainless exhaust elbow. The bend in the exhaust elbow brought the exhaust line too close to the thru-hull of the water separator outflow. A small cut was made and the tube was carefully bent and welded to enable the exhaust run to stay well clear of the thru-hull. Having an identical stainless steel spare made in the field will cost about $100-$200 US — not much.
Late in the testing, we had a problem with the New Zealand made BEP marine ANL fuse block installed on the genset frame. It melted and broke the fuse. After a couple days of research, we realized the 125 amp fuse (and 125A spare fuse provided by the factory) was providing too much resistance (125A fuse on 200 amp alternator). It heated up the single shared fuse and wire terminal post (mounted in a plastic support) to the melting point. The plastic port melted, twisted the fuse, broke the ceramic fuse cover, and melted the inside of the plastic BEP fuse block cover before breaking the fuse. We may have contributed to the heat-up by using stainless steel washers between the cable terminals and the fuse. As we learned, stainless is not a great conductor and may have contributed to the failure. We changed to a 200 amp fuse and upgraded the fuse block to a Blue Sea 750amp ANL model. This works really well and stays nice and cool.
An installation review
In late April, our friend, Todd Rickard, from Seattle visited New Zealand and stopped in to see us in Opua. Todd is the person that originally installed the Fischer Panda. He inspected Duncan's install and made a few suggestions for improvement. Now, we have several small projects to do on rainy days in a tropical anchorage somewhere.
Postscript
Lots was learned during the installation...
The issue with the alternator not putting out 14.7 volts was a big time-sink for us. It is possible the field wire was knocked loose in-transit or during installation, but there should have been some sign of connection to the negative brush — there wasn't. If a wiring diagram was provided from the manufacturer, the problem could have been identified the first time Duncan took the alternator off and found the broken wire hanging there. If we had carried the unit off to a qualified New Zealand electrician on day-one, we would probably have had it working a week sooner. We would also have kept the Sterling stuff, having never asked Sterling for documentation and support information.
If Duncan had installed a DCGen more than once, the install time would come down dramatically. A skilled installer could have done this in a week and would have had fewer troubleshooting issues after the install.
This install invalidated all of Fischer Panda's previous blame-the-installation red-herrings. The new unit uses all the original Fischer Panda exhaust system (1.5" 20 Ft exhaust hose, 1.5L water lift muffler, same water separator), fuel system (with one intake line upgrade), wiring, and raw water cooling/anti-siphon solution installed in 2001. The new generator works great, runs consistently well, and burns very clean. The old Fischer-Panda was a lemon. Period.
Well, how do we like the DCGen 482?
With over 90 hours on the genset, we are still very happy with it. It's simple, appears to be very reliable thus far, and puts out some decent amps. We have only a few minor issues that are all compromises we knew about and were willing to accept.
First, it's a bit loud — maybe 2-3x louder than the old (1-cyl) Panda. Robin said it sounds like a lawn mower sitting just outside. We could look at options to get the sound level down (they offer a sound shield), but we are already getting used to it — so probably not. We've even looked into a simple sound insulating thermal blanket that would just velcro over the engine itself, but it would end up being custom and likely expensive. Our engine room insulation is sufficient.
Another idea would be to add a manual or automated throttle control to "turn down the volume" and reduce fuel consumption as the demand from the alternator tapers off — but this all adds cost and complexity. We will continue to live with it the way it is at a fixed rpm. It's still much quieter and more efficient than a 76 HP Volvo running at 1500 rpm driving our small Balmar alternator and generating only 70 amps!
The 180 amps or so output from the Prestolite alternator is sufficient for the batteries, but 250 amps would have been nicer. 200 amps is about right for this size engine and leaves some headroom for belt driven accessories. The Onsite Power DCGen 722M (3-cyl) may handle a larger alternator, but we just didn't have room for it in the engine room.
The Genie 280/12 solution from Ample Power, with basically the same engine as the DCGen 482, belt drives (therefore at a higher rpm) a 280 amp alternator. Of course, then you have the additional concern of pulley alignment, as well as belt wear, slipping, and tension setting. You also don't have a platform to drive accessories. A Genie 280/12 might be a good option if you have a large battery bank or Gel/AGM batteries that can handle high charge rate (up to 30% of capacity). We are okay with the DCGen482's 180 amps and can fully recharge our 745 Ah bank (when discharged 250 Ah or so) in less than 2 hours of run time.
So far Duncan's ecstatic with the simplicity and ease of maintenance of the Kubota 482 engine. With the transverse mounting everything is right there and within easy reach (although you still must lay over the main engine). It even has a real oil filter and the oil stays clean for many hours (the Panda oil turned tar-black 10 minutes after an oil change). We had a minor oil leak at the oil pan gasket early-on, but tightening the pan seems to have stopped it for now. If it is still a problem down the road, we will have Onsite Power fix it when we get to Australia. The 482 exhaust is also very clean and we are no longer spewing black soot into the anchorage through the water separator! Someday, we may add a few Murphy gauges (engine temp, exhaust temp, oil pressure) to assist with troubleshooting, but if the generator never has any trouble, maybe not.
Another minor suggestion is to move the relays and fuses out from under the fuel bleed screw, oil dip stick, and coolant drain-cock. These electrical bits might be better off located away from all the potential drips. It wouldn't be that difficult to move them off the unit altogether.
Well that's about it for the DCGen 482. The DCGen is a well-constructed, simple, and solid unit that works as advertised — after resolving the few initial glitches. We will post on the blog if anything changes, but all is well on Whisper's electrical front. The batteries are happy and behaving exactly according to the Toyama specification. The charging system is working very well now, with a smooth temperature-compensated charging curve. It shows diminishing returns on the charge when it gets down to about 40 amps in, so we only do an 80% charge and let the solar handle the rest. The Kubota engine reliability looks great so far, and fuel consumption seems right for the load. Also, we have done much less over-cocktail-hour complaining about generators than at any time in the last six years.
After completing the genset installation and the varnish projects, it was time to celebrate. Time for some bubbles and nibbles.
Now, go get ready to go!
With this major work behind us, it is time to provision and prepare for the passage. We left Ashby's after three weeks, tested everything at anchor for two weeks, then returned to a mooring in Opua to start getting ready for the passage to Fiji. The socializing begins while we wait for weather windows to open. Enough work! Let the fun begin!